a blog by someone who spells bad and writes even worse SO read no more if you cant deal with it
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Thursday, April 22, 2010
Out with the big dogs today this tube is coming OUT
So in some kind of lucky break i came across the right size 1.75 cutting tool and adapted it to fit by cutting jig
I had to cut 1/2 inside and 1/2 outside so the tools mandrel would stay supported and allow it to cut
So now i can order a new tube and with a bit of grinding epoxy in a nice leak free tube
Allmost fixed it but the new section had a blister
Sunday, April 18, 2010
The stern tube contuines
I have know since i pulled the prop-shaft and the cutlass bearing was worn through a a few degrees angle there was and aliment issue :rolleyes:
So out with the cutlass bearing and in with 1" bronze bushings and aliment shaft
Well i am pretty sure the stern tube was in the right place and the motor was 3-1/2' high SO that left the famous a MONKEY did a bad job of installing the strut
The wood really was on its last legs anyway so i am looking at as a blessing
The FEIN make quick work of that mess
And like magic suddenly everything lined up PERFECT now i just have to clean up all the parts and make some epoxy shims so i can lock it down in aliment
So out with the cutlass bearing and in with 1" bronze bushings and aliment shaft
Well i am pretty sure the stern tube was in the right place and the motor was 3-1/2' high SO that left the famous a MONKEY did a bad job of installing the strut
The wood really was on its last legs anyway so i am looking at as a blessing
The FEIN make quick work of that mess
And like magic suddenly everything lined up PERFECT now i just have to clean up all the parts and make some epoxy shims so i can lock it down in aliment
The hatch is allmost done
Wednesday, April 14, 2010
seafevers singel biggest nightmare
The shaft log which is one of those last ALMOST forever parts is broken and the PO pretty much had the shaft seal held in with plumbers putty
So this jig was made up at the motor height and i have to shim it up in line with the Prop Strut which is the part outside the boat that holds the prop shaft using a long shaft
Then i can cut out the bad part and epoxy in a new one which is so easy to type and so hard to do :)
Monday, April 12, 2010
a post about various progress
One of the bigger issue with the motor was changing the FWC impeller without draining 1.5 gallons of anti-freeze as ONE time was ENOUGH
So i found i needed 1/2' ball valves and 3/8 X 1/2 male nipples as the 3/8 valves were just to small
I had to tweak one handle to tighten the valve But there is enough there to open and close the valves once or twice a year :)
The hatch is back from powder coating and looks great and the waterjet place should have the lens cut this week as i HATE cutting and sanding plastic
I made two seacock mounting plates using the great Mainsail guide at
http://www.pbase.com/mainecruising/boat_projects
And for the final touch i pumped out 15 gallons a REALLY bad gasoline and got the tank out of the boat and called it a day on Sunday as i do have to work a real job :)
So i found i needed 1/2' ball valves and 3/8 X 1/2 male nipples as the 3/8 valves were just to small
I had to tweak one handle to tighten the valve But there is enough there to open and close the valves once or twice a year :)
The hatch is back from powder coating and looks great and the waterjet place should have the lens cut this week as i HATE cutting and sanding plastic
I made two seacock mounting plates using the great Mainsail guide at
http://www.pbase.com/mainecruising/boat_projects
And for the final touch i pumped out 15 gallons a REALLY bad gasoline and got the tank out of the boat and called it a day on Sunday as i do have to work a real job :)
Saturday, April 10, 2010
progress
A lot of slow steady progress is being made BUT i forget the camera :)
The forward hatch came back from being powder-coated and looks great i am just waiting to cut the new lens and then put in in DOW 795
The motor is ready to come home as soon as its not raining
The forward deck core is coming along BUT its still to cold to work very fast as a second piece in one day will disturb the first piece if the epoxy has not full cured which is taking about 12 hours
On Sunday i plan to pump out the old gasoline and remove and inspect the fuel tank
The forward hatch came back from being powder-coated and looks great i am just waiting to cut the new lens and then put in in DOW 795
The motor is ready to come home as soon as its not raining
The forward deck core is coming along BUT its still to cold to work very fast as a second piece in one day will disturb the first piece if the epoxy has not full cured which is taking about 12 hours
On Sunday i plan to pump out the old gasoline and remove and inspect the fuel tank
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